I forced a 1/2 mm steel wire coil spring into the tube to prevent it from getting crushed or kinked.
I wrapped a piece of 3/64" lead sheet around the valve to lightly increase its weight (+ 35 g) and get a good movement: +/- 90 mm for a free length of 95 mm. I used tin-lead solder to make it a tight cylinder around the valve.
The new flop tube is much more flexible, provides more than twice the previous flow area, but is 170 g lighter. Moreover, the Goodridge check valve is perfectly tight and opens at the lightest suction to a full 1/2" diameter.
All stuff comes from Goodridge and Mc Master-Carr. A lathe was necessary to adapt the Goodridge fitting and valve to the tube.
I wound the steel wire in the threads of a 12 mm rod and forced them together inside the tube, then unscrewed the rod which let a coil spring tight against the tube wall. The tube keeps its flexibility, but gets very strong.
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My previous flop tube was made of corrugated Teflon tubing, but of smaller diameter to get a good flexibility. Sometimes the oil pressure was low at idle when hot, probably due to the too small diameter. Making the fitting tight on corrugated Teflon needed a high pressure crimping, and with time the aluminium fittings got cracked and leaked.
Moreover I was using an original heavy flop weight, with an original one-way valve which I didn't trust very much, for tightness as well as flow capacity.
I got the steel wire from a local shop, but McMaster-Carr sells the same: 8860K11/12 for instance.
Gilles